rbradleymedmd
Go Kart Champion
- Location
- Columbia, SC
Well, the title pretty much sums it up. The reason I'm having difficulty understanding these logs is due to my inability to meet requested boost spikes; however, the rest of the pull is dead on with a (decreasing n75 duty cycle). Usually a standard boost leak shows a similar psi drop across the spam of the pull (corresponding with an increasing n75 %)...this is not the case here. I have yet to come across any logs that show similar results to mine (anywhere...any engine, any car).
With that said, below are six graphs (logs) from my car over the past 4 weeks. The first two are with the stock DV and APR's sII+ HPFP file, the car is running 100%...
The next two logs are the same file with the EJ DV kit installed (the timing/rail pressure log was to confirm there were no other circumstances affecting the boost pressure). The car was given three days to adapt to the new hardward before logs were taken...
The next log is the same file with the OEM DV reinstalled and the car was given two days to readapt back to the old hardware...
Finally, the last log is with the EJ DV reinstalled and no adaptation was allow...reinstall completed and logs taken immediately upon start-up (this has been by far the best log taken since the issues arose, but it's still not 100%).
My local guy seems to think that it's definitely an issue with the OEM wastegate...possibly some carbon build up. We plan to pressure test the system soon, but I have gone over every inch of the intake tract and there is no blow-by oil traces anywhere and all connections look stout. I have also run the Deviant Speed PCV fix to determine if my PCV was leaking and I noticed zero change via boost gauge (no logs taken). Thanks for any help. :thumbsup:
With that said, below are six graphs (logs) from my car over the past 4 weeks. The first two are with the stock DV and APR's sII+ HPFP file, the car is running 100%...
The next two logs are the same file with the EJ DV kit installed (the timing/rail pressure log was to confirm there were no other circumstances affecting the boost pressure). The car was given three days to adapt to the new hardward before logs were taken...
The next log is the same file with the OEM DV reinstalled and the car was given two days to readapt back to the old hardware...
Finally, the last log is with the EJ DV reinstalled and no adaptation was allow...reinstall completed and logs taken immediately upon start-up (this has been by far the best log taken since the issues arose, but it's still not 100%).
My local guy seems to think that it's definitely an issue with the OEM wastegate...possibly some carbon build up. We plan to pressure test the system soon, but I have gone over every inch of the intake tract and there is no blow-by oil traces anywhere and all connections look stout. I have also run the Deviant Speed PCV fix to determine if my PCV was leaking and I noticed zero change via boost gauge (no logs taken). Thanks for any help. :thumbsup: